-
Notifications
You must be signed in to change notification settings - Fork 4
Open
Description
I loaded the example code on my Arduino UNO and I have a 470nF capacitor between CLK and GND - this does not seem to be enough for proper de-bouncing.
Also I experience a much stranger issue - no matter which direction I turn my encoder, the value is always going up, it is never being decreased.
I tried with different encoders (of the same type) and they all do the same thing.
Am I missing something?
Those are the encoders I am using => https://www.amazon.de/gp/product/B07T3672VK?ref=ppx_pt2_dt_b_prod_image
Metadata
Metadata
Assignees
Labels
No labels